Improving Oxygen Transfer Efficiency in Chemical ETP
Improving Oxygen Transfer efficiency in a Chemical manufacturing plant
Background

A mid-size chemical manufacturing company situated in Madhya Pradesh was facing efficiency issues in improving oxygen transfer efficiency in its ETP, such as low efficiency, biomass suspension, and diffuser dysfunction. Despite maintaining a good overall diffused aeration system, their biomass was not developing, and MLVSS was very low.

As a result, the client incurred high CAPEX due to unnecessary diffuser replacements and remained non-compliant with regulatory COD/BOD limits.Facing challenges in improving oxygen transfer efficiency and facing high energy costs? Let Team One Biotech help.

ETP details:

The industry had primary treatment, biological treatment, and then a tertiary treatment.

Flow (current)750 KLD
Type of processASP
No. of aeration tanks1
Capacity of aeration tanks1150 KL
Challenges: 

Parameters Avg. Inlet parameters(PPM)Avg. secondary system outlet parameters(PPM)
COD180006000
BOD85002800-3000
TDS300002500
Problem Statement:

The client observed persistently low dissolved oxygen (DO) levels in the aeration tank despite extended blower run-times and increased air supply. This resulted in:

  • Sub-optimal biological treatment
  • Elevated energy costs
  • Occasional odor issues and inconsistent COD/BOD reduction

A preliminary diagnosis indicated biofilm accumulation and diffuser fouling, affecting fine bubble formation and limiting oxygen dispersion.

Our Approach

Team One Biotech initiated a comprehensive on-site audit including:

Diffuser Health Check

  • Inspected diffuser membranes for fouling
  • Identified scaling and microbial slimes affecting pore performance

Baseline Monitoring

  • DO levels across the tank: <1.5 mg/L
  • Specific Oxygen Uptake Rate (SOUR): <15 mg O₂/g VSS/hr
  • Blower energy use: ~65 kWh/day
  • OTE Baseline: Estimated OTE was 12%

Microbial Evaluation

  • Floc structure was loose, with filamentous dominance
  • Low settleability (SVI > 200)

To implement a cost-effective, eco-friendly bioremediation strategy that:

  1. Enhances the degradation of formaldehyde and glutaraldehyde.
  2. Restores biological treatment efficiency.
  3. Achieves compliance with CPCB norms.
Solution

We proposed a 2-fold intervention:

1.Application of T1B Aerobio Bioculture

  • Dose: 10 ppm daily for 10 days, 8 ppm for next 10 days, and 5 ppm for next 10 days, then 3 ppm as maintenance every day.
  • Objective: Enrich native microbial diversity and improve biomass quality T1b Aerobio bioculture solution by improving oxygen transfer efficiency

2. Aeration System Optimization

  • Conducted sequential backflushing of diffusers
  • Realigned blower duty cycles with microbial demand using DO automation feedback

Monitored DO, pH, and ORP to ensure a stable environment.

Results:

After 60 days of implementation:

Parameters Before interventionAfter Intervention
DO in Aeration Tank1.2 mg/L2.8 mg/L
SOUR1             3.6 mg O₂/g VSS/hr22.3 mg O₂/g VSS/hr
SVI210 mL/g120 mL/g
COD Reduction72%87%
Blower Runtime24 hrs/day16 hrs/day
Energy Use65 kWh/day38 kWh/day
OTE12 %21.4 %
Application results before and after

Conclusion

With the combined effect of T1B Aerobio bioculture and technical aeration optimization, the client achieved a 78.3% increase in oxygen transfer efficiency. This translated into:

  • Significant energy savings
  • Improved microbial activity and settleability
  • Stable effluent quality, meeting compliance standards

This case demonstrates how biology-driven solutions, coupled with system know-how, can deliver tangible performance and cost benefits in industrial wastewater treatment.

Ready to optimize your ETP performance? Connect with us today

📧 Email: sales@teamonebiotech.com

🌐 Visit: www.teamonebiotech.com

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